forked from luck/tmp_suning_uos_patched
iio: imu: inv_mpu6050: fix suspend/resume with runtime power
Suspend/resume were not working correctly with pm runtime.
Now suspend check if the chip is already suspended, and
resume put runtime pm in the correct state.
Issues seen prior to this were:
When entering suspend, there was an error in logs because we
were disabling vddio regulator although it was already disabled.
And when resuming, the chip was pull back to full power but the
pm_runtime state was not updated. So it was believing it was
still suspended.
Fixes: 4599cac846
("iio: imu: inv_mpu6050: use runtime pm with autosuspend")
Signed-off-by: Jean-Baptiste Maneyrol <jmaneyrol@invensense.com>
Signed-off-by: Jonathan Cameron <Jonathan.Cameron@huawei.com>
This commit is contained in:
parent
e450e07c14
commit
0a2bf9200a
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@ -1617,6 +1617,10 @@ static int __maybe_unused inv_mpu_resume(struct device *dev)
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if (result)
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goto out_unlock;
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pm_runtime_disable(dev);
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pm_runtime_set_active(dev);
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pm_runtime_enable(dev);
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result = inv_mpu6050_switch_engine(st, true, st->suspended_sensors);
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if (result)
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goto out_unlock;
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@ -1638,13 +1642,18 @@ static int __maybe_unused inv_mpu_suspend(struct device *dev)
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mutex_lock(&st->lock);
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st->suspended_sensors = 0;
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if (pm_runtime_suspended(dev)) {
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result = 0;
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goto out_unlock;
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}
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if (iio_buffer_enabled(indio_dev)) {
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result = inv_mpu6050_prepare_fifo(st, false);
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if (result)
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goto out_unlock;
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}
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st->suspended_sensors = 0;
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if (st->chip_config.accl_en)
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st->suspended_sensors |= INV_MPU6050_SENSOR_ACCL;
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if (st->chip_config.gyro_en)
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